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May 2002

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Subject:
From:
Mike Wallace <[log in to unmask]>
Reply To:
SouthEast US Scuba Diving Travel list <[log in to unmask]>
Date:
Thu, 23 May 2002 21:22:46 -0500
Content-Type:
TEXT/PLAIN
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TEXT/PLAIN (415 lines)
Since this came to me with the recipient list suppressed I'll forward it on. 
Some of ya'll may have already gotten this as well....


------- Forwarded message follows -------
Date sent:      	Thu, 23 May 2002 20:56:26 -0400
From:           	Tom & Dee Scott <[log in to unmask]>
Subject:        	Spiegel Grove- The full story......
To:             	(Recipient list suppressed)

OK folks, I've been authorized to release this. It should hit the news 
tomorrow morning, media got it when I did, you get it now. You also get it 
all as they won't print the full statement, just their take on it.

Read it for yourselves, decide for yourselves. What follows is the final 
report of the man who was hired as "Sinking Supervisor" for this event. 
This report was NOT edited. All questions as to what went wrong should be 
answered here.

Formatting might get a bit hosed as it was copy/pasted from a Word 
document. Should be readable, if not, contact me for another copy.

Tom Scott

---------begin---------

SPIEGEL GROVE AFTER ACTION REPORT
20 May 2002
Prepared for: Spencer Slate
By: Ken Normand


	I have been representing myself and continue to do so at this time.  The 
following report was completed after I returned from Key Largo, 
Florida.  The tragic roll over of the Spiegel Grove was indeed 
heartbreaking but most importantly no one was hurt or killed in the 
process.  This report will list the following:

(1)	The original sinking planned agreed upon in Virginia Beach, Virginia on 
April 23, 2002
(2)	Approximate time lines associated with concrete events which occurred 
during the operation
(3)	A brief synopsis of why this operation went wrong

The facts presented here are from my notes and explain in some detail the 
most important events that I was involved with and voice concern over.  The 
report is written to the best of my recollection and knowledge of the facts.



1.  On April 23, 2002 the following personnel were present at a Spiegel 
Grove meeting held at Bay Bridge in Virginia Beach, Virginia: Rob Blesser, 
Jon Dodrill, George Garrett, Dave Score, John Halas, Don German, Ken 
Normand, Claude Thompson, Ray Salopek, Dave Purdy, Larry Leonardson, and 
Spencer Slate. This was only the second meeting that I was able to 
attend.  I was available by phone or email at all other times and was 
contacted multiple times about different items of concern.
We discussed many aspects of the Spiegel Grove from cleaning it to sinking 
it.  Each person involved had an opportunity to speak on his part of this 
sinking operation, what would be required and a chance to answer any 
questions or concerns.
	I discussed my plan to direct holes to be cut for water entry and air 
exit.  My original sinking plan had contained many things that would be 
covered in Rob Blesser's over all plan so bits and pieces of my plan were 
extracted to make an over all guide.  The actual part of the sinking was to 
be directed by Slate and myself.  All plans were subject to some 
modification and it was agreed upon that such change could possibly be 
needed.  This was accepted by all.
	The flooding plan that was agreed upon was as follows.  I wanted to keep 
the well deck dry and free of water.  Cut 8"holes in the wing walls from 
frame 52 -250 every five to eight feet at the deck level to help facilitate 
water flow. Cut multiple holes in frame 52 well deck bulk head for water 
surging in at flooding time.  Open every tank top through out the 
ship.  Cut holes in the main deck to let air out as water came in from the 
underside.  Cut holes in ballast tanks connecting them together and 
allowing water to free flow forward.  I agreed to ballast down some 
internal belly tanks to help reduce the need for so much water to come in 
and sink the vessel.  I also stated that I wanted to have holes cut along 
the outside skin of the ship but would wait until the sinking day to do so 
to prevent accidental flooding in addition to cut holes from frame 228 aft 
on the final day to prevent accidental flooding.  I used a copy of the 
docking plans to explain all of this and even acquired my own personal copy 
to study, review and suggest changes if necessary.  I said that the ship 
would look like Swiss Cheese after the cutting of the necessary holes on 
the outside and inside the well deck.  I received thumbs up on this 
proposed plan.  I answered all questions and concerns and had no doubts 
that we could do this safely and effectively but that preparation would be 
the key to success.
	I inspected the anchor system again and concluded that one of the ships 
large winches was in the locked position because each machine had a 
different visual appearance..  Each winch was in a different configuration 
and I concluded that one anchor would not drop.  I did not think that the 
brake alone was holding the anchors in place and that the pelican hooks 
should be installed for the tow.  Don German volunteered to handle the 
anchor process and also agreed that one winch could possibly be in the 
locked position.  I recommended that the anchors weight be lowered onto the 
chain stoppers and pelican hooks to verify that the brakes were working and 
that the winches were not locked.  I am unclear of exactly why the system 
was not tested but the port anchor would not drop when the brake was 
released and therefore resulted in a delay of the anchoring process.




2.     14 May 2002   Boarded ship by accommodation ladder on starboard side 
early afternoon. Ken Normand first aboard. Visual inspection revealed ship 
had good tow.  Slight list to starboard.  Stern gate was still secured fast 
with all pins in place.  Pins were knocked out with not much effort.  The 
last latch located on the port side was very tight and the steel was cut 
around it to help lower the gate.  Gate slowly lowered half way down then 
slowly creeps into full open position within the hour resting on its 
holding bracket..
1300  Inspection of spaces below main deck.  All hatches and scuttles had 
to be broken free of welds.  All lower compartments were relatively free of 
water.  Aft engine room had 6'' of water in bilge.  Rudder room was clear.
1415 Masson Keeter and Ken Normand/   Tug slacks off pull.  Tied tow
bridle with ½ rope to remove strain.  Removed bridle and let tug pop strain 
line and tow bridle free.  Tug secures line back to ship for final movement.
Ken Normand and Spencer Slate/  Starboard anchor chain was let off brake to 
hang on pelican hook. Anchor dropped approximately 3 feet in the haws 
pipe.  Brake was resecured.  Pelican hook was released with a sledge hammer 
when directed over GPS marked buoy by Masson Keeter.  Brake was slowly 
released and anchor fell with control to the bottom.  Brake was applied to 
slow chain release.  Anchor locked in place with approx 300-400' of chain 
deployed.
		1430 Port anchor would not drop due to locked windless motor.  The anchor 
detail became very confusing and unorganized.  I left the bow after to many 
people became involved with the process.  I inspected the stern anchors to 
ensure the shackles were moused and safety wired.
		1500  Some well deck hatches were removed and then replaced for tank 
inspection.  All tanks appeared to be free of debris and or liquids. The 
after most tank in the well deck had approx 10% water.  This was pumped out 
to a forward belly tank designated by Ray Salopeck.  I concurred.
		1600  Supplies are delivered to the stern gate(fire hoses, pumps, tools, 
food, drinks, safety equipment, etc)  I was informed that starboard anchor 
was let off brake and chain ran out to bitter end.  Approx 900' of chain is 
now out on starboard.
		1630 Removed emergency tow line from rear port closed chock.
		1700  Port stern anchor was routed through the inside well deck 
chock.  This anchor had 300-400' of cable and one shot of chain.  This 
cable was rerouted to the port aft closed chock as planned.  The stern 
anchor was rigged for pull out by John Debruce, Dave Debruce and their crew 
from Upper Keys Marine Construction to the tug boats bow and drug out the 
stern gate as planned.  Tug was directed to pull anchor to the starboard 
side with the cable obstructing the stern gate and planned exit and entry 
point of the operation.  (incorrect action)
		1730  Starboard stern anchor was disconnected from the starboard aft bit 
and relocated to the port bit that was already occupied by the port 
anchor.  This smaller anchor had approx 150' of cable and one shot of 
chain.  (incorrect amount of cable)  It was noted to the project manager by 
Spencer Slate and myself that this was not the planned four point 
moor.  This act now put the ship in a three point moor. The water was 10' 
below the well deck at this time.  Command and Control (CC) aware of the 
incorrect  and unplanned mooring procedures.  Ship still at slight list to 
starboard.
		1800 Ray Salopek directs torch man to cut hole in aft ballast tank and in 
rear bulkhead of aftermost 940 ton tank.  This was done from inside the 
rudder room.	
1800-2130  More pumps were brought aboard and the center main tanks
were pumped with sea water. One tank was at 95% and the other at 50% when 
we secured for the night.  All operation halted at 2200.  Ship has good 
trim and list.


15 May 2002   0800- 1900 Diver safety cutting was performed by all welders 
and
  cutters.
  0830  I noted that well deck water was leaking into the aft ballast tank 
through  the rear most well deck hatch.  I replaced that tank top.  I 
informed Dave Debruce, the pump supervisor that this hatch could sink the 
ship and it should be watched and guarded with extreme caution.  He assured 
me that he would seal it with a rubber gasket.  I periodically checked the 
rudder room for additional leakage from that hatch. The water was 7' from 
the well deck at this time.
  0900  Informed Command and Control that 4 personnel would be performing 
an underwater hull inspection to check for soft patches.  Inspection 
revealed 3 soft patches, slight oyster growth and a clear discharge for the 
main condenser.  Divers clear fouled line from tug Portsmith's port screw 
after hull inspection of Spiegel Grove. CC notified of dive results.
1100 Large quantities of water are now being pumped inside various tanks
directed by Ray Salopek and Claude Thomas.
	1300  Claude Thompson, Justin Lowd and myself record draft readings of the 
ships freeboard from the following positions  on the main deck in this 
order: starboard midship, starboard aft, port midship, port aft, starboard 
forward and port forward.  Thompson lowered the plum tape, Lowd verified it 
was touching the water and I recorded the actual numbers on paper for 
Thompson.    After review of the numbers, I was comfortable that the ship 
was not in danger at this time but that the displacement was increasing 
every hour water was pumped in, and the pressure increasing on the existing 
leaks raised their flow. I handed the information back to Thompson.
1500  Water is now 5' from well deck.  Rear tank hatch is secured with rubber
gasket and bolted lid.  Salopeck and Thomas direct various wing wall tanks 
to be flooded.  I disagree because this will prevent the cutting of the 
well deck bulk heads at some spots and prevent water travel and air 
escape.  I discussed this with Command and Control personnel.  Multiple 
tank tops are still in place throughout the ship.  Cutting the diver safe 
entry still has the priority.  Water is still being pumped into the wing 
walls.  Fill holes will not able to be cut as planned in the proper 
tanks.  The over flow lines are draining some water over the side.   Some 
ballast tanks are leaking into unknown spaces through out the 
ship.   Addition tanks are directed for flooding at midship.  CC is notified.
1600 Dave Debruce informs me every two hours of the condition of the rear
hatch.  He clearly understands the danger of that hatch failing.  I have a 
torch man cut two 8" holes, two feet above well deck port side at rear 
escape trunk,( Frame 229) to facilitate detonation cord for Friday.
1700 -Rudder room is now taking on water through the rudder post seals into 
the rudder room. (approx 50 gal per hour each)  Tank top is still secure 
aft of rudder room.  The water is draining below deck (where 
unknown.)  Engine rooms are taking on water through the stern tube and out 
of the shaft seals. (100-200 gal per hour.)  CC notified of above.  Midship 
belly tanks are leaking into aft engine spaces and other lower spaces.  CC 
notified.   Some leaks are repaired in ballast tanks from inside the engine 
rooms.  Forward engine room takes on water through an open valve from a 
ballast tank.  Valve secure by Justin Lowd.  No significant water in 
forward engine room at this time.  Aft engine room continues to slowly 
fill.  CC notified through out my routine inspections of engine rooms and 
rudder room.  Well deck is now ballast 3' above water.  Water is washing 
into the well deck and over the sealed hatch.  Dave Debruce reconfirms that 
it is sealed.  I double check it from below and determine that we have a 
good seal.  I again explain how critical and important this hatch is.  I 
told him and his dad that this hatch would sink the ship if water were 
allowed to free flow inside to the rear 940 ton tank and smaller tanks 
aft.  This tank is now starting to fill from the water that is not staying 
in other tanks through out the ship.  This small amount of water is not 
impacting the draft aft at this time.  Estimate rear tank has 50 tons of 
water inside.  Capacity 940 tons.  CC notified of stated conditions.


16 May 2002  0900  Wave conditions are so bad that we cannot board from the 
stern and must use the ladder again.  The tug was surging up and down 
5-10'.  Very dangerous conditions.  I immediately made my rounds once 
aboard and discovered the rudder post water intake had increased to approx 
100 gal per hour each and the aft engine room was taking on approx 1" per 
hour.  Shaft seals were leaking at approx 200-300 gal per hour.  In 
addition to the shaft seals leaking, the ballast tanks were adding water to 
the aft engine room.   Some of these leaks were not able to be seen or 
heard. Forward engine room was still in fair condition.  Flooding was 
limited to the shaft seal only.  CC was notified.  Ray Salpoek confirms we 
are still in good condition.  I feel that the ship is naturally taking on 
enough water, and we should evaluate and throttle back on pumping the next 
tanks to be flooded.  Salopek disagrees.  Pumps are having trouble 
delivering water to forward large tanks so water will be hopped from 
midtanks to forward.
		1000  I informed Salopek that I would be instructing cutting operations 
through out the main deck and well deck bulk heads.  He disagreed and 
informed the project manager.  The project manager called a meeting of all 
supervisors to discuss a plan to finish up and stay on schedule.  I stated 
that I needed to cut vent and fill holes as my sink plan read.  I would 
also have a list of critical holes to be cut for Friday.  I wanted to 
secure pump operations very soon and start offloading gear at 
1200.  Salopek and Thomas disagreed and said they intended to partially 
fill the well deck with 2' of water.  I immediately voiced my concern and 
reminded them that I was the sinking supervisor.  Rob Blesser defended 
Salopek and Thompson.  I told everyone in the CC that if they flooded the 
well deck that the ship would sink itself and possibly roll over.  Claude 
Thomas then began to review his version of the plan.  I tried to input my 
concern that he was making a positive block for the water and air by 
filling the wing wall tanks and I was shut down.  I then verbally told 
everyone that I would not be making any decisions involving the flooding 
process and would place the demolition charges were directed by Salopek and 
Thompson.  Forced Flooding continued through out the day.  Many people 
asked me for direction and I told them to see Salopek and Thompson and that 
I was no longer in charge of the flooding. I pulled Rob Blesser to the side 
and had words with him about my disappointment and lack of concern for the 
approved sinking plan that had been discussed and approved.  He could only 
offer his apology and was not willing to take my concerns as 
serious.  George Garrett broke this meeting up when a helo was inbound.  I 
had no more to say to the CC at this time.
		1330  Billy Poe of Explosive Services Inc came aboard.  He briefed the CC 
that when they finished up pumping, cutting and welding he would take over 
and place the charges.  He also stated that I would help determine the demo 
placement.
		1400 Engine room tour with demo guys.  Demo placement was decided.  We 
would place Poe's shape charges on main discharge pipes and intake 
valves.  Ray Salopek concurs with the demo plan.  Engine rooms are still 
taking on water.
		1430 Blanking plate is removed by Justin Lowd and Spencer Slate on main 
36" valve to be blown.
		1500  Demo placement is marked with spray paint by Ken Normand and Justin 
Lowd.
		1600  Normand and Lowd continue to make rounds forward and aft.  Multiple 
hatches are still secured on the starboard side.  Multiple hatches, 
scuttles and doors are secured forward.  Very few vent holes are cut from 
frame 1 to frame 150 main deck down.  Few vents holes are visible forward 
below main deck.
I have torch man cut small openings in well deck bulk heads in engine room 
escape trunks on both sides to facilitate detonation cord placement on 
Friday.  Frame 110 port side and Frame 154 starboard side. CC notified of 
holes cut for detonation cord. Pumping continues.  I am now finding water 
in multiple voids below deck that had been dry days before.  Ship is 
sinking by itself.
		1800  I depart the ship with other personnel down a rigged gang 
plank.  Water is within a foot of the well deck.   Pumping is planned to 
continue until 2200.  Pumping is secured at 1900 as reported to me by Dave 
Debruce later that night.  Dave Debruce informs me that we still have water 
tight integrity aft.  We discuss the importance of the rear tank and hatch 
again.


17 May 2002  0930 -0950 I was meeting with Billy Poe and his crew at 
Atlantis Dive Center firming up the demolition plans when we got word that 
the ship was sinking.  We immediately left Atlantis Dive shop and headed 
out.  When we got in sight of the ship we could see that the stern was 
already low in the water. It was reported to us to have taken on 10' of 
draft aft in 5 minutes.
0950-1015 The bow raised up out of the water and the ship began to roll to
starboard.  We could see this from 3 miles away.  When we finally got on 
station the ship had come to rest on its stern upside down and the air 
filled bow protruded above water.
		1100  Additional holes had been cut in the wing walls at frame 230 at the 
deck level.  This would allow water to enter the large rear tank.  We 
relocated to the tug to formulate a demo plan to vent the bow and was 
informed by Dave Debruce that Ray Salopek and Claude Thomas had directed 
him to remove the rear most well deck hatch that was already 1' 
underwater.  He declined several times, explained that it would sink the 
ship and was ordered to remove it anyway because their calculations said 
the ship would stay afloat.  The end results were exactly as predicted by 
the original sinking supervisor.

		

3.	In conclusion, I feel that this roll over could have been prevented days 
before it
ever happened.  The mishap started from the rush to get the ship to Key 
Largo without testing the anchor system, acquiring the right lengths of 
cable for one stern anchor and not following the sinking plan agreed upon 
at the meeting.
	The testing of the anchors could have prevented the chains from running 
out farther than needed.  The port brake system was not nearly in as good 
shape as the starboard.  It took three men to turn the brake wheel on the 
port.  This led to the initial confusion and could have resulted in injury 
experimenting with the anchors out at sea when this could have clearly been 
done safely in the harbor while in a controlled environment.
	The next incorrect procedure was the stern anchor detail.  The cable was 
to short for the small balance fluke beach anchor on the starboard 
side.  The port anchor was first to be rigged and was directed to be placed 
running across to the starboard side.  This had the cable at an angle 
across the well deck.  This anchor had one fluke, a shot of chain and the 
right amount of cable and could have been a very valuable holding point but 
was instead pulled the wrong way.  The starboard anchor was then removed 
from the starboard side and placed on the port.  Its deployment was at the 
right angle but its insufficient cable made it practically useless.  The 
next day the ship had swung to port setting the bigger anchor and making 
the small one just an unused clump.
	Slate and I questioned this incorrect procedure with CC and was told that 
they were trying to compensate for wind and current.  Their intentions were 
good but the bigger anchor should have been moved over to the starboard 
side and it would have set itself fine with the right angle of pull and 
also left the well deck open for easer access.  This was not an after 
though, it was suggested on the spot.  An anchor on the starboard stern 
could possibly have prevented the starboard side from rolling inboard 
causing the vessel to lay upside down.  The larger anchor should have been 
placed starboard and was originally suggested.
	The last action in question was the blatant disregard for the agreed upon 
sinking plan.  I   made my intentions very clear at the meetings and 
through out each working day.  My recommendations were seldom met.  I chose 
to wait until the day before flooding to have the vent holes cuts but was 
positively shut down.  This is why I chose not to have any say so in the 
flooding and sinking plan as of Thursday May 16,2002.  I choose to assist 
the demolition guys with their permission on charge placement.  My plan to 
cut multiple vent holes would have let air out and water in.  The direct 
action of removing the hatch that had been deemed so critical all week was 
actually what made the ship sink on the spot.  It flooded the rear end of 
the ship that was water tight holding up the back of the ship.  The ship 
would have sank by itself probably during the weekend because of the large 
amount of water that was pumped in and the amount of water that was coming 
in on its own but proper vent holes would have let the air out.  I actually 
thought for a moment as it was going down that it might just land on the 
bottom alright but when the bow rose up so high in the air it was evident 
that there was not enough ballast forward and no vents to let the air out 
in sufficient time to prevent a roll over and subsequent air entrapment.
I walked the ship everyday all day and used my eyes, ears and senses to 
help me make some of my decisions.  My other tools of success were frequent 
draft readings aft where the water would be coming in first, water tight 
integrity checks at critical places and constant monitoring of the large 
amount of water that was being pumped in.  This excessive amount of water 
pumping was not necessary due to the fact that we had permission to use 
explosives to cut water entry holes.  I agreed to some ballasting during 
initial planning but at some point you will reach the straw that breaks the 
camels back.
	
	I am sorry that this had to happen this way and thank GOD that no one was 
hurt or killed during this mishap.  Equipment can be replaced, a human life 
would not have been.  I explained and emphasized the inherent danger 
involved with this type of operation and made it very clear to all 
involved.  I thought I had everyone's trust and confidence with this 
matter.  It is my belief that this could have been prevented.  We had 
proper planning but had poor cooperation.  I would like to thank the people 
of Key Largo Florida and Spencer Slate for believing so highly in me and 
giving me an opportunity to participate in such a valuable, worthwhile 
cause.  I think that a salvage company will be able to make this situation 
right and I personally have gained a multitude of operational experience 
from this mishap but have to say that this is the first one that I have 
been involved with that has gone turtle on the surface.   I express no bias 
opinion and have stated the facts as I have witnessed them and have drawn 
my own conclusions.
Good Luck and Blue Skies.


					Respectfully,
K. C. NORMAND
----------end------------------


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__ 
Mike Wallace
Huntsville,Ala

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